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Hello!
In a brand new board loaded and working with the hack I decided to unsolder the hall sensor wires and instead put some pins in order to connect the plug directly to the board.
Now it is running rough as you can see in this video
I have already checked continuity from the motor sensors to the processor and everything seems ok.
Any ideia on were to look next?
Thanks
The text was updated successfully, but these errors were encountered:
Hello!
In a brand new board loaded and working with the hack I decided to unsolder the hall sensor wires and instead put some pins in order to connect the plug directly to the board.
Now it is running rough as you can see in this video
I have already checked continuity from the motor sensors to the processor and everything seems ok.
Any ideia on were to look next?
Thanks
The text was updated successfully, but these errors were encountered: